Buzzie made it to Goodwood! We had a great weekend rubbing shoulders with the motorsports gliterati at this famous track. I’d love to tell you that the Douglas DT engine ran perfectly over the weekend, blowing away the Norton and JAP powered opposition. Sadly the reality was a bit different! But we had a great time and Buzzie with her Douglas power unit attracted a lot of attention.
The headline is that the car failed in the practice and in the race itself. However we were granted a second chance to complete a flying qualification lap, which she did without issue. The problem with the engine was the same each time, which was that the exhaust valve pushrod adjuster on the rear cylinder shortened itself until the rocker end leapt out of the socket on the rocket. The same thing had happened in a test run on a local airfield the week before.
It took the three occurrences for us to work out exactly what was happening and that it wasn't due to component failure, wrong clearance adjustment or failure to lock the adjuster properly. There were a couple of people we met who actually owned DT bikes, and neither of them had heard of such a thing happening.
So if anyone has any experience of something like this happening, and what can be done to stop it please reply below. I am all ears !!!